Well it was a shake down, first time out in bout 5 years or so.. prob really closer to 6, but hey.. and everything has changed, not just the suspension, but literally everything.. normally you shake the car down after a single upgrade, but this has literally pretty much the whole car has been replaced.. even the frame I’ve modified to be able to fit the low slung diff carrier.. everything…
So really the only expectation I had was not to catch fire, explode for blow the engine up.. and we came, we went ,and we saw, and didn’t do either of those 3 things.. so that’s a huge plus.. even ,huge-er was the fact that the frame, together with the diff and carrier , steering modifications and the compete Frankenstein-ed suspension worked together like it was always meant to be.. I am seriously over the moon with how the car handles and behaves. The brakes are unbelievably awesome..
The thing that wasn’t awesome is that the car was down on power..
And that’s a big one, less power than I had when it was NA with its carbon CSL intake and tune.. much much less.. the car would pull fuel at somewhere between 5200 and 5600rpm.. not sure on the exact numbers there, but I have my theory’s. Are they correct? Nfi, I’ll find out when I fix what ive pulled apart atm, but my guess is that the belt is too long, due to having an uprated 72mm pulley and I’ve got the bloody stock belt.
That’s my guess.. that the belt was slipping at low rpm and then really slipping at high rpm (which is why the belt halfly fucked off when it had had enough of that) and thus causing such a fuel rich mixture that the car couldent cope. Not sure if it actually went into limp mode at that stage, but there you go, so I motored around, under 5k rpm, but that was difficult esp in corners..
Just to give you an idea of how much power was down, I was only able to change into 6th at the end of the straight , (keeping it under 5k rpm) heavily on the brakes into turn 1, where as previously , I’d be winding the pajesus out of 6th on the main straight.. I don’t wanna give a time on that as I wasn’t recording.. but it was slow.. still had a lot of fun in the tight twisties, but I can only dream of how this will go when I sort this issue out. (We! Thank you, both me and Josh are on it)
But yeah, I’d recon the culprit was the belt, I’ve since ordered 3 new belts, each 5mm shorter than the last, starting at 6pk2334. I gotta download Josh’s new software and then sign up for another track day when I’ve got this bad boy back together. It’s in pieces atm tracking down some intake piping leaks.
Again, it was an AWESOME day, so much went really right, so much so that I had a huge grin on my face, even when I was swapping fuel as I thought maybe it’s pulling fuel due to old dead fuel.. gotta try something right.. (I didn’t figure out the belt slipping until the day after in the middle of the night when that out of nowhere and came to me like a revelation)
But yeah, even though the SC had issues, it still was a huge success, even just in how the car handeled.
The snag list aside from the engine isn’t too extensive, the most important one on their probably being the overheating of the thermonfan switch. I HAVE to fix that. That’s dangerous as it could cause a fire inside the cabin.
The massive outstanding parts that iam most happy with has to be the Penske rear coilover conversion and the brakes and steering. The steering kit from MRT is such a joy.I can’t comment too much yet on the rear diff, as it didn’t miss behave at all, but then I didn’t push it that hard either yet.
Again, we didn’t crash, didn’t explode or catch on fire.. it was a GREAT day!!