Well the rain stopped at last.
Steering wheel off, lower column shroud off.
Driver's seat out - a must, as I was able to lay upside down with my feet up on the roll hoop and see what I was doing.
I read through firebobby's thread which proved invaluable.
Decided to see how far I could get with minimum disturbance of other stuff.
Good news is, just under 2 hours from starting, the motor is out and ready to go to ECU Testing.
I didn't loosen any column bolts, or remove anything else. There was just about room to wiggle it out.
Only issue was I had to push the clutch pedal right to the floor as the motor jammed up against the top of it.
Plenty of loom length so you can lower it into the well then disconnect the plugs where you can see what you're doing.
Only word of caution there is the plastic coated black wire. It is tie-wrapped to the motor and these need snipping to let it hang down fully onto the floor, so have snips ready as it's not good to leave it hanging while you go find them.
My only Torx sockets are 3/8 drive which was too bulky. However, an 8mm socket fits perfectly. I used a bi-hex ratchet ring spanner to break the initial torque and after that a 1/4 drive ratchet, socket, extension and UJ.
I have a feeling the rebuild could prove a bit fiddly to line up those two bolts but as the motor pushes into a recess on the side of the column you can get it in position safely without having to hold it there.
So post off first thing Monday morning and hopefully get it back to refit next weekend.
Steering wheel off, lower column shroud off.
Driver's seat out - a must, as I was able to lay upside down with my feet up on the roll hoop and see what I was doing.
I read through firebobby's thread which proved invaluable.
Decided to see how far I could get with minimum disturbance of other stuff.
Good news is, just under 2 hours from starting, the motor is out and ready to go to ECU Testing.
I didn't loosen any column bolts, or remove anything else. There was just about room to wiggle it out.
Only issue was I had to push the clutch pedal right to the floor as the motor jammed up against the top of it.
Plenty of loom length so you can lower it into the well then disconnect the plugs where you can see what you're doing.
Only word of caution there is the plastic coated black wire. It is tie-wrapped to the motor and these need snipping to let it hang down fully onto the floor, so have snips ready as it's not good to leave it hanging while you go find them.
My only Torx sockets are 3/8 drive which was too bulky. However, an 8mm socket fits perfectly. I used a bi-hex ratchet ring spanner to break the initial torque and after that a 1/4 drive ratchet, socket, extension and UJ.
I have a feeling the rebuild could prove a bit fiddly to line up those two bolts but as the motor pushes into a recess on the side of the column you can get it in position safely without having to hold it there.
So post off first thing Monday morning and hopefully get it back to refit next weekend.
